|
Case History #1 Wax Plant
Destroyed by Fire
We were instructed
to investigate the cause of the
fire. The starting point of the
project was to interview all
personnel involved and to sift
through and examine the physical
remains of the wax plant furnace
to ascertain the cause. The
investigation demonstrated that
the fire resulted from the failure
of the support lugs of an air
inlet cone in a centrifugal forced
draft fan.
The cone and the
lugs were manufactured from pure
aluminium. The impeller of the fan
had 16 vanes and 1500 rev/min.
Therefore, the fundamental
aerodynamic forcing frequency on
the support lugs was 400Hz. This
induced 34.56 million stress
reversals per day. The fan failed
approximately 10 months after
commissioning, therefore, the lugs
will have experienced 10 billion
cycles from commissioning to the
time of failure.
We were not able to
calculate the dynamic stress to
which the support lugs were
subjected in order to determine
the probable number of cycles to
that such a material could have
sustained within its S-N curve to
predict the fatigue life. However,
it is known that pure non-ferrous
alloys including pure aluminium do
not exhibit a fatigue limit or a
lower stress level at which it may
operate for an infinite number of
stress reversal cycles. Therefore,
there is a finite number of stress
reversals that will always induce
a fatigue failure.
In support of this
view we found the 10 lugs
which had been supporting the air
inlet cone. All of them were
broken into two parts with one
half welded to the air inlet cone
and the other half bolted into the
casing of the fan. Two of them
exhibited catastrophic tensile
failures but eight exhibited the
classic characteristics of fatigue
failure on the failed surfaces.
This was determined by microscopic
metallographic analysis.
The Client took our
findings to the Fan Contractor who
denied liability, rejecting the
findings in our report. However,
by coincidence, a colleague in the
hydrocarbon processing industry
happened to meet Dr Stoneman some
two weeks after the matter had
become an impasse. By chance the
two discussed what they had done
since they last met. The colleague
who was working on a new furnace
project with a number of forced
draft fans manufactured by the
same company, which had not yet
been commissioned. The colleague
told Dr Stoneman of a peculiar
development that the fan
manufacturer had come to site one
day and without explanation had
dismantled all the fans to replace
the air inlet cones.
The dispute between
the Client and Contractor was
resolved shortly after with the
contractor accepting total
liability for the cause of the
fire!!
Case History #2 Roller Coaster
Disaster
Whilst returning
from a business trip to Germany Dr
Stoneman sat by a lady who was a
Barrister defending an action on
behalf of an Insurance company,
holding liability for the
consequences of the failure of a
roller coaster. A number of people
were killed in the disastrous
failure.
Whilst describing
the technical issues it was felt
that the technical arguments being
provided to the Barrister were not
valid. We were engaged to review
the issues and advise accordingly.
There were two issues related to
financial liability. The first was
the fundamental physics of the
cause of the mechanical failure
and secondly, at what part of the
design and commissioning processes
did the error occur.
The first issue
required a judgement of the
failure process and extensive
technical analysis to demonstrate
that the mechanical component that
failed was inadequately designed
to fulfil its function. That was
the relatively easy part.
The second issue
was more important to the Insurer
client as they were responsible
for faults in the Commissioning
but a second Insurer was
responsible for any fault in the
Design. We argued and successfully
demonstrated that the fault was
one of fundamental design and so
the liability of our Client was
relieved.
Case History #3 Oil Industry
Cherry Picker
A workman was
injured when the tension chain
that supported the boom of his
mobile elevating work platform
otherwise known as a Cherry Picker
failed. The chain catastrophically
failed and allowed the boom
supporting his work cage to
retract without support falling a
distance of more than 40
feet.
The workman
suffered substantial physical
injuries and financial damages
from his inability to work in his
well-paid employment within his
trade in the Oil Industry. He sued
inter alia the employer,
the Cherry Picker hire company and
the Cherry Picker manufacturer.
All denied liability and
retaliated by endeavouring to
attribute blame on the other
parties to the action.
It was claimed that
the injured Claimant was accused
of contributory negligence by not
using the Cherry Picker properly,
causing the chain to overload and
fail.
The Hire Company
was accused by all sides of not
having maintained the machine
adequately, allowing shot blasting
grit to accumulate such the chain
was overloaded by fouling from the
shot blasting grit.
The employer was
accused by all sides of not
providing adequate instruction to
the Claimant on the use of the
Cherry Picker.
Finally, the
manufacturer was accused of
providing a machine that was not
fit for purpose by their not
making provision for the design to
prevent fouling of the tension by
shot blast grit.
All sides
vigorously denied their various
accusers, especially the
manufacturers. However, we judged
that the design of the boom
assembly was deficient in that any
foreign material that entered the
chain tube of the boom could not
fail to accumulate in and around
the chain, with the inevitable
failure at some time. On
investigation we found that new
versions of the Cherry Picker
incorporated a sealing system to
exclude foreign debris from the
chain. We requested disclosure of
the design records of the new
Cherry Pickers that the company
had manufactured since the
failure, to establish what the
reasons were for the known design
revisions. Disclosure of the
documents was resisted and the
case was settled by the
manufacturer making a "without
liability" settlement out of
Court.
Case History #4 Marine Mooring
Winch
An operator on a
marine jetty for an Oil Company
was severely injured when a steel
hawser on a pneumatic winch, broke
and lashed his body.
The winch was used
to haul marine mooring lines that
secure Very Large Crude Carriers
(VLCC's) to deep water jetties.
The operation involved one man
controlling the air winch whilst
the second man stood at the edge
of the jetty signalling to the
winch man when to apply load. He
signalled for the winch to be
started but soon after the mooring
line had cleared the rope running
launch it became entangled with
the structure of the jetty. The
second man called to the winch
operator to stop but the winch
operator did not hear him and the
winch was so powerful that it
loaded the steel hawser to beyond
it's breaking point. The elastic
energy in the hawser was such that
it sprang back and lashed the
man's legs and arms as he tried to
protect himself.
It was later
discovered that the winch man had
been distracted at the critical
moment and was not watching his
partner on the edge of the jetty
for a signal. It was also
discovered that the winch man a
hearing deficiency and so was only
able to receive visual signals,
which he could not do because he
was distracted, or very loud
audible signals.
These matters
contributed to the damage
sustained by the victim but had
the hawser not failed then no
damage could have occurred. We
investigated the mechanical
arrangement of the winch and
hawser and found that the ultimate
strength of the hawser was
approximately 1 tonne. However,
the tensile capacity of the winch
was 2 tonne. Therefore, the
situation existed that if the
hawser was ever constrained from
being hauled in, without an
adequate means of controlling the
winch, it was inevitable that the
hawser would be loaded to
failure.
On further
investigation it was discovered
that the manufacturer and
installer of the rope retrieval
system had consciously accepted
the situation winch following
complaints by the operators when
the system was first installed
that the original 2 tonne hawser
was too stiff and too heavy to
handle. The 2 tonne hawser was
therefore replaced with a 1 tonne
hawser without any protection
being provided that would prevent
overloading by the winch. The
situation had been operated
without incident for five years
but the coincidence of the design
weakness and the hearing impaired
operator produced a dangerous and
ultimately injurious
situation.
Case History #5 Navigation
Buoy
A new generation of
navigation buoy was deployed at
sea, with life expectancy of 20
years. After approximately 20
weeks they started to fail by
physical disintegration under the
dynamic loads imposed by wave
motion.
The buoys housed
solar panels for powering warning
lights and a horn, via two
large industrial
rechargeable lead-acid battery
packs. The batteries stored energy
to deliver power to the warning
lights and horn at night or when
solar radiation was
insufficient.
We examined the
failed buoys and found that the
structural capacity of the support
and encapsulating body were wholly
inadequate for the hostile
environment that they would
experience. Even a simple estimate
of the loads imposed by orthogonal
wave loading, from modest wave
heights, caused stress levels that
were likely to induce immediate
failure.
The problem was
made worse by fact that the
restraint system provided for the
batteries had little
strength. When the buoy was
impacted by a wave, the relative
inertia of the structure of the
buoy and the battery pack was such
that the batteries exerted loads
that caused their restraints to
fail.
This in turn
allowed the batteries to be thrown
around inside the supposedly
weatherproof enclosure of the buoy
that housed the control gear for
the solar panels and warning
systems. The batteries first
destroyed the electrical
equipment, rendering the warning
function of the buoys inoperable
and then continued to cause
further damage to the structure,
in some cases puncturing the
enclosure allowing seawater to
enter.
We judged that the
fundamental design was defective
and so the client claimed damages
against the designers and
manufacturers. The issue was
settled without going to
litigation.
Case History #6 Flutter
Instability in Heat Treatment
Furnace
A new heat
treatment furnace for steel sheet
functioned by blasting the steel
sheet with jets of air from 25000
nozzles to cool the sheet at a
pre-determined rate. The system
failed because the air blast
caused the sheet to oscillate
violently such that it came into
contact with the nozzles. The
nozzles were variously damaged or
dislodged and the steel sheet
product was damaged beyond
recovery. The cost of lost
production was estimated at £1
Million per day.
It was thought that
the flutter phenomenon was due to
an aerodynamic instability within
the system. We were asked to
measure the aerodynamic
characteristics of a mock up to
determine if we could reproduce
the instability. Using specialist
anemometry and flow visualisation
methods, we determined that the
aero-elastic properties of a
tensioned flat steel sheet
positioned between two sets of
elastic jets, were susceptible to
a flutter type phenomenon.
In collaboration
with colleagues, we went further
to investigate whether the flutter
phenomenon was able to be reduced
or at least controlled by the
physical characteristics by the
disposition of the cooling jets in
relation to the tensioned flat
steel sheet. In the event, we
demonstrated that if the angle of
the jet impinging on the surface
of the steel sheet was taken from
orthogonality, to an off
centre-angle of approximately six
degrees, then the flutter-energy
feedback loop was destroyed and
the oscillatory motion of the
steel sheet ceased.
Therefore, in
seeking the underlying cause of
the problem, we also produced a
potential practical
solution.
|